Tuesday, 10 March 2020

Dashboard part 5

Next part of the dash was to cut the holes in the leather for the instruments and switches ,but first took it back to the car to make sure it still fitted and yes it did  ,again followed others blogs and cut the hole onto segments so they will fold back .
After trying various methods found the best way was to use a scalpel bought from the internet and cut the gauges into 12ths
the switches very  fiddly and cut them into 8ths as well as multiple cuts to my finger.

cutting leather  with scalpel and hopefully not the floor  
Once this was all cut out tried all the gauges in to make sure that they would still fit and found that the indicator lamps would not go in ,gingerly use of the dremmel sorted this and pushed all the lights and gauges in .
I then applied glue to the segments and stuck those to the back of the dash.
segments glues
Had to push the switches in from the wrong side to make the segments stick and then hopefully will be able to put them in the right way .
well pleased and going for the rev counter on the drivers side

Throtle Cut out part 2

Needed to tidy the cut out as the carpets will be going in soon.
Seems an absolute age since I cut it out and got told off by Andy at GD for doing so .
So please be warned he does not agree with cutting this out nor is he very happy when he finds out but as I have already done it and got told off I figured I will stick with it
cut out from last year with the 2 throttle body screws
 I removed the pedal gear after we had set the throttle up in order to figure out were the carpet will need cutting. before attempting my first attempt at fibre glassing.
It appears to be like everything else easy when watching someone else but doesn't seem to go as well on the day .
Put the inner skin back in the hole with resin and glass fibre  mat to take up any differences and then glassed in round the edges .
went well considering I was working one handed just waiting for it to go off so I can tidy it up .
pre clean up as still tacky


Tuesday, 25 February 2020

DashBoard Part 4 and Bits

Its leather time , Was really dreading this part as it could go wrong very quick and is the focus point to the car .Started by laying the leather at the bottom and making sure that the bottom was going to fit
I glued the bottom in place and let it dry .
Next day came to the rest and started by stretching the leather up which seems to require 3 pairs of hands ,By good fortune had to leave for another task and came across a local furniture upholsterer,the conversation came round to my dash and a asked for any tips ,His reply was amazing ,bring it in and I'll do it for you. So I did and he only charged me beer money .

All my own work !!
   Another couple of little jobs tackled  was to blank off the two unused  ports on the engine .
Jubilee clip added to stop the cap falling off
Spare air box connection
This one I tapped with a 6mm tap and then stud locked a 6mm grub screw .

Also managed to finish off the heater pipes .

just grommets required

Undertray

On a recent visit to GD I noticed that one of the cars had a radiator protector fitted .
I thought it was a good idea so came home with one and the aluminium under tray. 

Ally under tray
the tray  fastens on the same bolts as the radiator so to save taking those out again I slotted the holes    when I came to try it in place it didn't fit (surprise) but because it fits in a tapper it was I case of take a bit off try it take a bit off try it etc .
the radiator protector was a similar story as in the laser cutting it warped and made marking it on to the top radiator bracket a challenge to say the least.




laser cut protector

Once in however it looks well worth the work .


The bottom is secured with 5mm bolts with washers to make up the difference but after twisting my sons arm he applied his lathe skills and made me some spacers !



Ah La Connor (thanks Son )

Tuesday, 4 February 2020

Dashboard Part 3

Next stage was to cut out the foam where the gauges need to be ,read other blogs and coped the idea of using a craft knife .This worked for the gauges but did not work for the switches or lights.
Came up with the idea of heating up a screwdriver and using it as a hot knife worked a treat .
dash hole cut including the additional hole for the heated seat 

Next thought I ought to look at the dash loom expecting it to have little labels on like the engine but no such luck .
Found myself looking at the build manual technical files and found the layout schematic and had to go though each plug and group of wires to identify them separately what a pain .
spaghetti with my masking tape idents  
This raised 2 issues  the first is there was no connection for the courtesy lights on the loom ( the wires just stopped at the plug ) .
the second was that there was a sender wire for the oil pressure  gauge but my gauge is pressure driven with an oil pipe .
Following the wire back though the looms it went to the unused wire at the back of the engine .



unused white oil pressure switch wire at top of picture
    I understand why there isn't an oil light as I have a gauge but .... if its there --  bought an adapter ring from ebay (£1.00) and then pestered my local motor dealers for an oil pressure switch to fit it ,result eventually and a huge thank you to Parkers (the parts people) ,switch that fitted  was from a Chevrolet Matiz( part number SOB807).

oil pressure take off with adaptor and pressure switch


   My idea now is to wire this in on the dash to the illumination on the start button ,my thinking behind this is when the ignition is on the start button will light up and go off when the engine starts .




Heater

Realised that after I had installed the heater there is another wire to go though the bulkhead to fasten on the battery It is the feed wire foe the ECU and fuel pump .
I was never totally happy with the heater pipe anyway as it seemed a bit tight in the hole and had the potential to wear though and empty the coolant so out it came to make the holes bigger .

Heater removed and holes made bigger
At the same time I noticed that the positive cable was not long enough to fit on the terminal and still look neat ,this was because I had routed it clear of the exhaust  .My solution was to fit a Battery isolating switch this comes with a removable key should I feel the need .

Battery switch fitted  and cable looks better



At the same time I thought it would be a good idea to have isolating valves on the heater circuit in case of a leak and also if I ever wanted the heater to blow cool air ( unlikely I know ) so ordered to valves from car builder solutions and happy with the fit.
the valves  have a flow arrow on so one is the wrong way round
which I will turn when I figure out which is the return pipe





Monday, 27 January 2020

Dash board part 2

after cutting 2 holes out for the heated seat switches thought better start with the Dash board .
Haven't been looking forward to this but cant put it off any more . .First I mounted the dash with the 5mm screws to make sure it still fits and then removed the screw one at a time to epoxy them in place .Once this had dried removed the dash and laid it next to the foam .Reading other blogs they glued the netting side of the foam to the dash so I copied that and seemed to work fine .
I made sure that the foam doesn't come round at the bottom but overlaps at the top as other builders.
Happy with the result so far will let it dry now before cutting out the holes .
Spray glue applied and lined p with the bottom captive bolts can be seen
This bits gone well



NumberPlate bar

Was told it would be easier to fit this bar before the body went on and then promptly forgot .
Again very difficult to try and get a measurement so opted for  the string between the 2 indicators .




string as a level
and then it was just a case of making it the same distance from the front .
Happy

Saturday, 25 January 2020

Bonnet Gas struts

Fitted the bottom bracket in line with the cross member underneath the car as it was an easy way to get them the same distance from the front as finding a place to measure anything is a challenge in itself
Bottom bracket bolted in place

 then I marked were the gas strut would come to on the bonnet in its retracted position added 10mm and that is were I will but the top bracket .
All the marks made sense at the time
 then it was just a simple transfer to drill the top bracket
Fitted

I was told by Andy at GD to put one ram on ad let the gas out until the bonnet just wont stay up and that should be right when I do the same to the other one , but tats for another day



Wednesday, 22 January 2020

Horn

I was always going to fit air horns like most other cobra builders but also wanted to be able to use the horn at times with people dying of shock .Guessing that there will be a delay before the air horn starts hit upon the idea of having a smaller horn as well so just a blip would only sound the little one . only time will tell if this works .

Stobel Air horn ready to be fitted

Little horn fitted under the header tank
Plan to put the Air horn relay on one of the 2 spare rivnuts  in the picture