Friday, 26 February 2021

Throttle cut out

 Once we had fitted the seat it became apparent that the pedal s were to high and driving would be very uncomfortable .pedals out and back like the Hokey Cokey  .

After the final fit there would be no advantage to having the throttle cut out i have previously done . So i have fiberglass the foam back in ,this will make the carpet a bit easier to fit (hopefully )

Foam glassed back in 

Dash board part 7

 Been to GD and got a replacement Start button and at the same time got advised that the button will not carry the intended start current !!! 

So Relay now required , fitted the relay on one of the gauges ,as per a previous post i intend to use the engine start light as an oil pressure light so this means that i will need to supply a feed to the light an then the iol pressure sensor will evevitivaly earth it putting the start light on when there is no oil pressure ie engine stopped .

Relay can be seen attached to fuel gauge with the feed coming from the volt gauge  
The gauge lights i have fitted using male spades for the positive but the negative i fastened to the gauge nus to try and increase the earth paths  
Left the speedo and tacho Gauges out to make it easier to fit the dash (hopfully ) 




 

Roll Bars part 7

 On to the last bit of roll bar fitting definitely  a 2 man job  and one that again needs to look right ,the holes are pre marked with 3 dimples to aid drilling,


 Had to be aware of were to place the hole in order to be able to get to the back of the bolts .After much deliberation we decided on on hole in the center, so marking bewteen the roll bars to give a centerline drilled the holes trough the rubber and body in one hit .found the easiest way to do this was by using the flex attachment of the dremel with a 3.2mm drill .

bracket in position ready to be drilled 

drilled and bolted down 

thought that was the final fix but not happy with the covers as the machine marks can be seen and not 100% sure that the rubber will seal so going to take them out again to polish and apply some sealant  Part 8 should be the final fix .







 

Wednesday, 9 September 2020

Roll Bars Part 6

 After much debate on what to fill the bars with went for the original idea of foam like everyone else ,Found some high density expanding foam from screwfix ( other brands available !!!) and used that . 

first wet the roll bars and then discovered that the tube is not linked at the weld so needed to fill that bar separately .

Used an extension tube on the foam to make sure we got all the tube filled ,sorry no pics as such a messy job .then put the bolts back in to protect the threads .

 


Once this had dried is was back in the car again to check the final fit in order to gat the bars to sit parallel had to place 2 washers under the rear bar on the left hand side .

I have opted for the single head rest support which needs to be drilled in the rear downpipe .



using a piece of string we were able to find the mid point so the head rest would look central.
Drilling them was an absolute nightmare ,Tried my cheap drill first unsurprisingly no luck .closely followed by the drills I bought at Stoneleigh again with limited success,then after much abuse from Steve he arrived with his "decent drills" and sorted .


 happy with that but unfortunately managed to scratch the top of the roll bars, so needed to take them out again to be re polished, Huge thank you to John at Alpha circle (Grimsby)  for sorting them out for me ,   

and so 

 its on to fitting the rubber seals and cover plates .

The outside cover plate needs bending to follow the contour of the car and after  much thought bending it round a scaffold tube seems to work the best ( need to remember to bend it first before drilling the 4 mm hole to secure it other wise the ring will kink on the hole. 



bent and ready to be bolted down .

Monday, 15 June 2020

Dashboard Part 6

After labeling the wires it still just seemed like a maze.
Set to and started at the hazard switch end.
Needed  the technical files section for the wiring diagram from the GD disc then hoped the rest would sort of  fall into place .
I have a key switch separate from the steering column and the  hazard switch were Andy at GD puts his so guessed  the wiring would reflect this.  
Key switch and hazard switch as a starting point 

Hazard switch wired and connectors for the stalks  

Next was to tackle the switches I noticed there was a cut out at the top and I didn't want to see that so mounted the switches upside down
The cut can just be seen 

I then had to sort out the wiring as the light switch and the heater switch are both 2 position but the side lights to stay on when headlights are selected .
sorted this out with my meter and came up with
connections for the switch upside down 
Will require a link wire between 1 and 2 
once the switches were done most of the wires dropped into place ,I had a couple of issues  first is the illumination of the start button I needed to be the oil pressure wire so had to lengthen  that ,
Some of the gauges didn't have the terminals marked up so used a 12volt source to check and at the same time checked all the lamps (and found the start button doesn't light up )
 and I had no wiring diagram for the speedo or tacho in the box . the tacho was straight forward once I looked on the web but the speedo is not so easy -email to Andy then .

Starting Again

Who would have thought that half way though March our world would turn upside down ?Still cant believe it ,
The whole car building process just got put on hold with all the other things going on but now can finally get  a bit of time back on the car .
Fitting the battery seemed to be an easy  next step
Didn't like the bracket idea as less holes in the bulkhead seemed to be the way forward to me  ,trip to the scrap yard and got a battery strap off a car that I think will work fine .
Battery cradle fitted with my strap secured to the back fastening  

Battery fitted  ready for cover plate to go on 

Tuesday, 10 March 2020

Dashboard part 5

Next part of the dash was to cut the holes in the leather for the instruments and switches ,but first took it back to the car to make sure it still fitted and yes it did  ,again followed others blogs and cut the hole onto segments so they will fold back .
After trying various methods found the best way was to use a scalpel bought from the internet and cut the gauges into 12ths
the switches very  fiddly and cut them into 8ths as well as multiple cuts to my finger.

cutting leather  with scalpel and hopefully not the floor  
Once this was all cut out tried all the gauges in to make sure that they would still fit and found that the indicator lamps would not go in ,gingerly use of the dremmel sorted this and pushed all the lights and gauges in .
I then applied glue to the segments and stuck those to the back of the dash.
segments glues
Had to push the switches in from the wrong side to make the segments stick and then hopefully will be able to put them in the right way .
well pleased and going for the rev counter on the drivers side

Throtle Cut out part 2

Needed to tidy the cut out as the carpets will be going in soon.
Seems an absolute age since I cut it out and got told off by Andy at GD for doing so .
So please be warned he does not agree with cutting this out nor is he very happy when he finds out but as I have already done it and got told off I figured I will stick with it
cut out from last year with the 2 throttle body screws
 I removed the pedal gear after we had set the throttle up in order to figure out were the carpet will need cutting. before attempting my first attempt at fibre glassing.
It appears to be like everything else easy when watching someone else but doesn't seem to go as well on the day .
Put the inner skin back in the hole with resin and glass fibre  mat to take up any differences and then glassed in round the edges .
went well considering I was working one handed just waiting for it to go off so I can tidy it up .
pre clean up as still tacky


Tuesday, 25 February 2020

DashBoard Part 4 and Bits

Its leather time , Was really dreading this part as it could go wrong very quick and is the focus point to the car .Started by laying the leather at the bottom and making sure that the bottom was going to fit
I glued the bottom in place and let it dry .
Next day came to the rest and started by stretching the leather up which seems to require 3 pairs of hands ,By good fortune had to leave for another task and came across a local furniture upholsterer,the conversation came round to my dash and a asked for any tips ,His reply was amazing ,bring it in and I'll do it for you. So I did and he only charged me beer money .

All my own work !!
   Another couple of little jobs tackled  was to blank off the two unused  ports on the engine .
Jubilee clip added to stop the cap falling off
Spare air box connection
This one I tapped with a 6mm tap and then stud locked a 6mm grub screw .

Also managed to finish off the heater pipes .

just grommets required

Undertray

On a recent visit to GD I noticed that one of the cars had a radiator protector fitted .
I thought it was a good idea so came home with one and the aluminium under tray. 

Ally under tray
the tray  fastens on the same bolts as the radiator so to save taking those out again I slotted the holes    when I came to try it in place it didn't fit (surprise) but because it fits in a tapper it was I case of take a bit off try it take a bit off try it etc .
the radiator protector was a similar story as in the laser cutting it warped and made marking it on to the top radiator bracket a challenge to say the least.




laser cut protector

Once in however it looks well worth the work .


The bottom is secured with 5mm bolts with washers to make up the difference but after twisting my sons arm he applied his lathe skills and made me some spacers !



Ah La Connor (thanks Son )